Finally put my goodies together with a handful of shots over the Chrony, time to share.
Goal is to achieve to between 900-1000 FPS with a .25 Syn rod shooting JSB Kings and PolyMags, be very quiet, refined, convert to Bull-Pup, enjoy.
Purchased new .25 Synrod. early last year. Cocking the gun was almost impossible, (
the ultra stiff, dragging cocking action that many new Synrods seem to be plagued with), with under 400 shots had more than a handful of double loaded pellets as result. Max velocity I could get out the rig with JSB Kings was in the 850's.
Ordered MDRL stock kit.
Ordered extra gauge block and .25" valve body to mod.
Ordered 10 lb and 12.5 lb hammer springs.
Ordered WAR NBH hammer.
Dad has a .25" Synrod so mods I performed were also done to his at same time.
Being a custom engine builder specializing in customer cylinder head building/porting/machining, applied some of the air flow improvement strategies to the Syn-rod using the Mill and lathe and hand tools, (
mind you, many of the strategies for engine performance dont "port" directly over to air gun valves/ports, pressure, dynamics, flows, etc are different). Dimensioned the factory valve body and poppet rendering it in A-CAD 2D to get a better idea how close some of the port relationships are, where material can be removed, and not be removed etc.
In short, the valve body work was a success meeting my goals thus far, though I admit with the WAR valve, all this effort and work is not something I will be doing again, WAR valve is the way to go.
Mods performed;
Gauge block bored out.
Factory Transfer port opened up to .154" ID.
.166" barrel port, slightly radiused in the pellet seat, (
pellet depth insertion for the pellets to be used verified deeper than port)
Factory valve body bored out to .500", region surrounding the poppet head opened up to 9/16" up to the valve seat for less valve-head shrouding. Bore behind the poppet opened up a skosch. Velocity port sealed with 2 part epoxy to fully eliminate the port and set screw installed, (
Epoxy locked it in), Valve body exhaust port opened up to .160", "carefully" radiused to throat to the valve seat port. Undercut the poppet valve stem behind the head and slightly radiused poppet head edges. Back side of valve body bored to accept small O-ring to help reduce pressure bleed that leaks pas the valve stem itself. Poppet spring replaced with soft spring just strong enough to hold the poppet close for filling from zero psi.
Main tube cleaned, chambered the gauge port in main tube to allow O-rings of gauge block and valve body to pass with less tendency to cut/shave the O-rings removing/installing from the filler end. Polished/buffed region of the hammer slide area, deburred the hammer bolt slot and sear slot. Heavy dose of DuPont Chainsaver w/Teflon on the hammer.
Cocking blot polished as well and breech bore for the cocking bolt, Slick50 ONE lube on the cocking bolt.
Divers Siilcone grease on all O-rings and air related components.
WAR No Bounce Hammer
Air Stripper holes opened up and angled forward.
2 holes drilled in 2 of the baffles flanks, those two baffles are first in line.
3 small holes drilled in base of shroud to allow venting of shroud pressure, Mr Clean Magic Eraser wrapped/crammed between barrel and shroud at base to damp the flow of pressure venting to the shroud relief holes.
Lawyer spring straighten out.
Valve body;Valve stem seal;Gauge block;